Basic covering is on... trim is next
Observations: The rebuild was good
amount of work and as per first impression, most of it confined to the
fueslage as the wing repairs took minimal time and effort. The
only issue encountered was the alignment of the prepainted trim on the
cowl and windscreen, due to replacing those parts with parts for the
Taylorcraft 20cc. The solution was to live with a slight kink as
can be seen in the trim striping as the cowl turns it down
slightly. The trim on the bottom of the windscreen had to be
overlayed to realign but that was easy.
Perhaps the most rewarding part of the effort was how easy the side
windows were to make after have fretted over what was to be done with
them. Also, the use of the lumberyard 3/16 plywood to rebuild
worked well.
The most significant observation regards the CG and a growing opinion
that the CG could have been too far aft and possibly the cause of the
crash. My reasons are that the heavy pilot seat was mostly aft of
CG (it has been omitted) but much more of an issue were the servo tray
and flight battery were in the aft cabin well behind the seat and they
weighed very nearly a pound and in the rebuild were moved a minimum of
6.25 inches forward to obtain proper CG. I just do not see that
the rebuild changed much about the structure weight. I'm tempted
to conclude that the PO (previous owner) wrongly balanced the plane by
marking balance points on the fuselage and taking the measurement from
the forward bulkhead where the wing dowels seat as is very typical of
most wings. One reason for this conclusion is that I almost did
it. The wing however has a 2.5" leading edge offset forward of
that bulkhead, which would cause a balance error of that amount.
Other observations are that the plane had been previously crashed and
that it had been flown very little as the engine and muffler were
almost spotless. It's possible that it had not been flown after
its first repairs.
Conclusion: The rebuild has been rewarding both from a standpoint
of enjoying the effort and financially. A good deal was gotten on
this plane as it was bought for $250 including engine, receiver and
servos. A new Slim Line Pitts muffler is $99 + freight
alone. The newly released version Taylorcraft is $549 for plane
only. The rebuild cost less than $100 and less than $75 if
one considers that only a small strip was used from a $26 roll of
checkered covering leaving the rest for another repair or another
project.
Final Report after flight testing.
Well.... the flight test was interesting. The engine had been
tuned following rebuilding the carb and seemed dialed in. It
started fine, a range check revealed no range or receiver RF issues and
the motor spooled up without any hesitations and seemed to be running
fine as it had when dialing it in a week or so before (it was a long
wait for a decent fly day). Take off was not much of an
issue. The nose wanted to rotate over a little and just a little
back stick settled it for a full run up and a slight bit more back
stick had her flying. She went right just a tad but otherwise
climbed smoothly. Two clicks of up and a click of left had her
about trimmed out.
After gaining altitude, power back to about half stick and checked for
trim at mid throttle... seemed good. Chopped the throttle (very
high) and let her glide and she seemed to enjoy a predictable smooth
glide. Powered her back up and looped her and that was smooth and
showed adequate power for a good size loop. Pulled a real tight
full elevator loop and she showed some tip stall character.... she'd
have to be respected. Up high at half throttle, she was put in a
45 deg down slope to test CG and she revealed only a hint of upturn
indicating the CG was probably exactly where it should be.
She was flying well perhaps five minutes into the flight and very high
down at one end of the field, the engine quit. Fish tailing her
back and forth didn't kill enough altitude and it wasn't long before
she was in trouble with too much height and a runway that went over the
hill and out of sight. She passed me 150 feet in the air. I
should have dived her and made a very hot wheel landing. Now, I
had a decision to make with neither option good. If I kept her
straight, I'd be landing her over the hill and blind and on a fairly
sharp downhill grade. If she caught a wing tip she'd cartwheel or
almost certainly without knowing when to pull the stick back, go hard
over on her nose and summersault down the grade. If I
tried to turn back on the runway, she'd likely stall.
I put the nose down and initiated a fairly hard turn to bring her
around and she tip stalled and went in on her nose from about forty
feet. She of course broke in half where all those windows are.
I didn't have any real good choices but the best would have been to
dive her hard and do a high speed wheel landing. Probably the
second choice should have been to land her blind and keep the wings
level until she was out of sight and then just hope for the best and
let her settle by herself. I admittedly chose the poorest option
but it is the one that I get away with on most of the models I fly....
this one however will not tolerate such behavior.
The Damage: She doesn't look as bad as the previous crash where
everything was destroyed from the aft cabin bulkhead forward.
There is very little damage forward of the forward cabin bulkhead and
no damage whatsoever to the middle of the cabin and rearward.
While she broke completely in half, she did so completely in those two
inches from the forward cabin bulkhead and into the windows. The
firewall, forward belly plan, windshield deck and landing gear blocking
are all intact. The only damage on the wing is to the two
mounting
dowels and one set of servo gears. The servo tray is not damaged,
nor are the wing struts.
Can it be rebuilt? Of course. How easy? I don't know
yet. She might can be pieced back together rather than a major
rebuild. I don't know how well the luan plywood can be fit back
into place. She is a very pretty airplane and the guys at the
field gave her a lot of chatter about how good she looked after the
rebuild. As can be seen in the above rebuild thread, it was a
major effort but would be some easier to do again. I've the
pattern for sides for example and now know how to make the side windows
with ease and have the molds for those. The greater question, is
she a plane I want taking up space in my garage or is she too
tempermental for my laid back flying desires and skills? My guess
is that I'll give her one more strike but I'm not sure that I'll
rebuild her now or lay her aside for a bit.
Why did the engine quit? I've no clue. I'd tuned it more
than a week prior to the test and did so after rebuilding the
carb. A bench run had shown that the carb had a problem because
the high speed needle was run in fully and wasn't leaning it out.
After the carb kit, it was run again and dialed in and the top end
needle was effective and normal. It was pulled back two hundred
rpm from top and had no spooling or idle problems. At the field,
it started easily, spooled without hesitation and run full power
without any sag. It ran flawlessly until she quit while cruising
at about half power. Did it heat up? I'd be surprised if
overheating was the cause of why it quit. The cowl was baffled
and there was plenty of exit. The most probable explanation was
the temperature and humidity difference between the day it was tuned
and the cooler very damp day. I doubt the temperature difference
was that big of an issue but combined with the humidity change, the
difference could have caused the flame out.
Repairs have begun and with luck, it
will be a fit the parts back together effort with perhaps a doubler or
two for added strength. A new cowl and windscreen are
ordered.
Mid January, 2010
While the crashed damage above looks bad, the broken parts have been
fit back together and repairs progress with only some doublers
remaining to be installed and then recovering the front section.
Those lower window panels will get closed in with plywood doublers to
add some mid plane strength. New windscreen has arrived but cowl
remains on back order.